
Lesson Learned on Electric Motor Shaft
A power station air compressor 750HP motor was sent to the motor shop for a winding
failure, refurbished and returned to the
station. Plant personnel performed a precision
alignment of the motor to the compressor,
yet high vibration was found on initial
startup.
Alignment
tolerances were reviewed, soft foot conditions
were minimized and motor mounting and support
adjustments were made to ensure no resonant
conditions existed. However, high vibration
levels were still found on the motor. Further
investigation of the uncoupled motor vibration
and phase identified a bent motor shaft.
Alignment
readings were all within tolerance for
the 3600 RPM machine. Soft foot problems
were minimal and were removed with step
shimming. Due to the extremely high vibration
readings in the order of 0.8 in/sec velocity
which was predominantly in the horizontal
direction, resonance was suspected.
An
investigation of the motor mounting structure
revealed a stiff, good supporting structure.
Bump tests on the motor found the natural
frequency well above and out of range of
influence by the motor operating speed.
Resonance was ruled out, so the unit was
started and phase data was taken.
Horizontal
readings found similar amplitudes of 0.7
to 0.8 in/sec at 180° out-of-phase between motor bearings. Much lower vertical readings were found
on the outboard (opposite drive end) motor
bearing of 0.02 in/sec and a high of 0.26
in/sec at the inboard (drive end) bearing
at 180° out-of-phase. Axial readings on the motor from one end to the other showed acceptable
vibration levels, but 180° out-of-phase. Phase readings across the coupling showed mostly in-phase readings
with low, acceptable vibration readings
on the compressor.
Misalignment
was suspected, but to rule out motor rotor
imbalance and a possible bent motor rotor,
an uncoupled motor run was requested. Vibration
levels were low vertically, but still somewhat
elevated horizontally for an uncoupled
motor, in the order of 0.1 in/sec at running
speed. Phase readings were mostly all in-phase
except for axial end-to-end comparison.
The difference in horizontal to vertical
readings along with the axial out-of-phase
suggested a possible bent rotor. Dial indicator
readings did find the motor stub shaft
bent by 0.009 inch at the coupling hub
mounting location tapering back to less
than 0.002 inch run-out near the shoulder
before the inboard bearing. The effects
of the bent shaft were greatly exaggerated
in the coupled condition resulting in the
coupled amplitude and phase readings mentioned
previously.

The
motor repair shop stated that they had
balanced the rotor to "as low as we could get it," however, we had not provided any balance criteria, nor had we requested any
vibration testing at the motor shop prior
to shipment. With the location of the bent
shaft, it is likely that the motor shop
would have never seen the effects of the
bent shaft with the rotor on a balance
machine. Shaft run-out tolerances were
never included as part of the repair specifications
by our company and none of the repair documentation
was provided by the motor shop.
Had
we requested shaft run-out checks during
repair and provided acceptance criteria
that included a final vibration reading
and analysis before the motor was shipped,
it is likely we may have caught this problem
at the motor shop. Now, we have no idea
if the shaft was bent during initial disassembly,
during shipment to the motor shop, while
at the motor shop or damaged upon return
shipment. We had no case for liability
against the motor shop, so the cost of
the repairs fell on us.
In
the future, we plan to specify balance
acceptance criteria, disassembly "As-Found" and "As-Left" criteria and request review of vibration signatures on repaired motors prior
to shipment. We are also developing job
plans for alignment work to include checking
shaft and coupling hub run-outs as part
of the initial steps to performing alignment.
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