January 20, 2005
Practical Case Studies for Maintenance and Reliability Professionals

Oil and Vibration Analysis Team Up to Save Electric Motor Bearings

This case study demonstrates how oil analysis and vibration analysis worked together to effectively increase the availability and reliability of a 300-horsepower vertical motor. The motor is used to pump sea water into a condenser that condenses steam after use in a turbine. Oil analysis found that the oil lubricating the motor's thrust bearing was contaminated with water, and vibration analysis confirmed the bearing’s condition and elevated the criticality of the alarm.

Vibration readings are taken on this equipment monthly. During April and May vibration readings fluctuated above alert levels, but did not indicate an immediate need for repair.

On May 30, oil analysis revealed that the upper bearing of the motor contained a large amount of water (see 5/30 column of oil analysis report).

A work request was made to change the oil at the next opportune time, and investigate the source of water ingress. A vibration reading was taken during this time to ensure the vibration trend was stable.

Over the next two months, vibration amplitudes increased over fault levels, and the oil change out was placed at a higher priority. At this time, we were confident that the water ingress was hindering the lubrication of the bearing, causing the elevated vibration levels. The oil was replaced on July 17, and subsequent vibration amplitudes decreased dramatically and remained below alert levels.

There may have been a time when advanced technologies competed with one another. However, in today’s work environment, it is vital that technologies complement rather than compete. If only vibration technology was used, this motor would have been subjected to higher vibration amplitudes, and the work request would have been made to inspect the bearing and equipment. However, upon inspection, the tradesmen would have found very little evidence of a bearing problem because the bearing fault was still in incipient stages.

It may also be possible that the water in the oil may not have been noticed and oil not replaced if the inspection was done by lifting the top cover. At the end of the job, the motor quite possibly could have been placed back into service only to find vibration levels continuing to be high. Coupled with oil analysis, the equipment was fixed and correctly put back into service.

Submitted by Cyril Ontai, Hawaiian Electric Company, Inc.

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